After I got the suspension dialed in thanks to the help of this great board, I wanted to get the motor more crisp. I live in Gainesville, 150 feet above sea level.
Here is what I did so far---
2005 200 stock everything, too rich everywhere. All testing done with Chevron 93 pump gas and Yamalube 2R 32:1
Rode the bike with a new 155 main and 45 pilot 2.5 turns out, removed snorkel but left the lid on with no additional holes.
Ran ok, still 4 stroked off idle and was generally sluggish so I ordered new needles from Sudco. CCM, CCL, BEM, BEL, AEL. I ran the 155 main but changed the pilot to a 42.
I ran the bike in the same conditions, fairly humid, 75 degree day. The BEM on the third clip was good until the bike warmed up, then it just four stroked, smoked and was weak throughout the whole range. I changed to the 1st clip and the bike responded better. Pilot was 3 out by this time.
I noticed that with the 42 pilot and the "L" needles, the bike ran waaay too rich and would not even powerband after fully warming it up. The best needle for the day was the BEM, top clip 3 out on the pilot.
I bought a 40 pilot on the way home and tried again this afternoon. The best I got today was :
152 main, 40 pilot, BEM 4th clip, 10 3/8" holes in the airbox lid, float height at 17mm, pilot screw out 2/3. I tried this combo once with the needle at clip one and clip 2 position, but bogged horribly in the midrange when whacking open the throttle in 2nd and 3rd, going walking speed. I tried the combo with the airbox lid off totally, which made the very bottom end real snappy part throttle with NO four stroking, but made the bike bog even worse in the whack test. Roll on was good if I rolled at a "medium" pace. Blipping also bogged bad. Lean bog, booowaaahh sound. I finally replaced the airbox lid and raised the needle to the 4th clip. The bike responded a lot better to the whack test in 3rd gear from near walking speed. I stopped here, as it got dark. I also ran a BR7ES plug for the entire test this day. Pulled it and it is still dark and oily like the 8 was. Top end was fine and pulled strong.
Hypothesis: I think that the bike likes a real lean bottom idle to 1/8th setting, but as soon as you whack the throttle, it needs to be rich to avoid a bog. I will try the BEL needle, which may be rich enough to avoid that bog when whacking the throttle off the bottom. I want to keep the 40 pilot in it for now and maybe add more airbox holes. I think I can get the bottom to not four stroke if it is lean enough. It's almost like the bike needs an accelerator pump! Any input would be appreciated. I know this will change a bit when I dump the stock pipe.
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