New '03 KDX200 with stock jetting smoked badly, suspected jetting was too rich:
- 32:1 Bel-Ray H1R
- choke lever NOT on
- air screw 1 turn out
- I have read carb jetting tips on JustKDX and Eric Gorr's site.
Replaced #48 pilot with #45 pilot and noticed some improvement, less smoke overall but still smoked quite a bit when I rolled on the throttle. Peppier response too. Air screw adjustment didn't seem to help.
Removed airbox snorkle, drilled several 1/4" holes in lid and test rode bike with #45 pilot (stock main jet and jet needle position). Smoked MUCH worse, smoke more grey than blue, engine made a throaty bass rev noise (didn't do that before the airbox mod). VERY sluggish response, definitely NOT an improvement.
Tried #42 pilot and noticed no improvement.
Went back to stock #48 pilot, still sluggish and smoked a lot, worse than before the airbox mod.
Finally, I went to a #45 pilot and a #158 main jet (jet needle still in stock position). This seems to be an improvement but definitely not "there"; lots of smoke when I roll on the throttle. Power is OK, better than before but not as good as I expected. Still got that throaty deep engine sound, though not quite as bad as before. My guess is it is still too rich, especially towards WOT.
Should I go to a #155 main jet? Lower the needle one position? I'm afraid of seizing the engine; what are the signs the jetting is so lean that seizing is a possibility?
The upside of all of this is I can disassemble a carb in no time...
- 32:1 Bel-Ray H1R
- choke lever NOT on
- air screw 1 turn out
- I have read carb jetting tips on JustKDX and Eric Gorr's site.
Replaced #48 pilot with #45 pilot and noticed some improvement, less smoke overall but still smoked quite a bit when I rolled on the throttle. Peppier response too. Air screw adjustment didn't seem to help.
Removed airbox snorkle, drilled several 1/4" holes in lid and test rode bike with #45 pilot (stock main jet and jet needle position). Smoked MUCH worse, smoke more grey than blue, engine made a throaty bass rev noise (didn't do that before the airbox mod). VERY sluggish response, definitely NOT an improvement.
Tried #42 pilot and noticed no improvement.
Went back to stock #48 pilot, still sluggish and smoked a lot, worse than before the airbox mod.
Finally, I went to a #45 pilot and a #158 main jet (jet needle still in stock position). This seems to be an improvement but definitely not "there"; lots of smoke when I roll on the throttle. Power is OK, better than before but not as good as I expected. Still got that throaty deep engine sound, though not quite as bad as before. My guess is it is still too rich, especially towards WOT.
Should I go to a #155 main jet? Lower the needle one position? I'm afraid of seizing the engine; what are the signs the jetting is so lean that seizing is a possibility?
The upside of all of this is I can disassemble a carb in no time...