dwcdds93 said:the pilot jet is 55, what the manual calls for. the new 360 jet works to almost solve the problem. it almost seems to run lean now at high throttle. it stumbles and runs rough. i adjusted the clip on the needle from 3rd to 2nd down, 4th down, and 5th down. it seemed to run the best on the 5th ring from the top. it was pretty cool outside when i was messing with it though. this could have something to do with the lean condition. i am going to pick up a few more jets to adjust it till it runs the best.
dwcdds93 said:i have been asking service people questions and one said it could possibly be the main bearing seal around the crankshaft and the another said it sounds electrical, like the coil is not functioning correctly under load.
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